Jurnal Teknologi Dirgantara
Vol.10 No.2 Desember 2012

EVALUASI KINERJA SAMBUNGAN PROPELAN PADA MOTOR ROKET RX 550 [EVALUATION OF THE PROPELLANT JOINT PERFORMANCE IN ROCKET MOTOR RX 550]

- Sutrisno (Pusat Teknologi Roket, Lapan)



Article Info

Publish Date
15 Mar 2013

Abstract

The propellant joints quality of RX 550 rocket motor using segmented HTPB propellant was become a debatable. In static test this rocket motor exploded and the nozzle was broken out at seven second after ignition. To evaluate these propellant joints the propellant installation in rocket motor was discused. The propellant joint strength was tested using Tensilon UTM III-100 test equipment. The rocket motor tube at the propellant joint position were marked and investigated before and after static test. The datas such as thrust and chamber pressure versus time were analyzed for finding the posibility of joints defect. Based on analysis it is found that the propellant joint can work well. The RX 550 rocket motor failure in static test didn’t caused by propellant joints. Key words: Propellant, Propellant joint, Static test

Copyrights © 2012






Journal Info

Abbrev

jurnal_tekgan

Publisher

Subject

Aerospace Engineering Chemical Engineering, Chemistry & Bioengineering Computer Science & IT Mechanical Engineering Physics

Description

Jurnal Teknologi Dirgantara (Journal of Aerospace Technology) is an Indonesian accredited scientific publication that covers topics of Rocket, satellite, and aeronautics technology, as well as a spin-off from aerospace technology, such as aerodynamics, astronautics, aerospace structure, power and ...