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Penurunan Waktu Changeover dengan Metode SMED di PT.Schneider Electric Manufacturing Batam-Plant Electro Mechanic Kristianto Wibowo Sudargo; felecia felecia
Jurnal Titra Vol 3, No 2 (2015)
Publisher : Jurnal Titra

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Abstract

PT Schneider Electric Manufacturing Batam-Plant Electro Mechanic is a company that produce electrical parts. Changeover time on some bench in production floor are very high, That’s why it needs to be reduced and improved. The method that will be used are Single Minutes Exchange of Dies (SMED) This project started with observing all machine on production floor, and after that some machine will be chosen to be improved. Changeover time data will be taken from this chosen machine, and this data will be analyzed with SMED. The result from SMED data will become suggested improvement for each machine. Suggested improvement that able to straightly be done will be directly implemented to target machine.Improvement on bench Auto Tampo Print was able to reduce the changeover time by 47%. Estimate improvement on bench Printing Body XB7-2nd Life should be able to reduce the changeover time by 75%. Estimate improvement on bench Manual Checker should be able to reduce the changeover time by 44%. Estimate improvement on bench Coil Winding and Testing MARSILI should be able to reduce changeover time by 18%. Estimate improvement on bench Coil Winding DETZO should be able to reduce changeover time by 7.4%.
Upaya Penurunan Kecacatan Painting Line 1 PT Astra Komponen Indonesia Yudha Kresna Primayoka; Felecia Felecia
Jurnal Titra Vol 3, No 2 (2015)
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Abstract

PT ASKI is motorcycle component manucaturer. The average of total NG products for 2015 is 23,64%, while for dirty spots is 11,4%. The company’s NG targets for 2015 are only 12% for total NG and 6% for dirty spots. Therefore Quality Control Circle (QCC) methods will be applied to reduce NG products. The root cause for dirty spots are dirty environment in painting line facilities and tools. Operators dicipline to keep the environments clean also contributes to this problem. Therefore this research suggest to change sprayman’s gloves and masking tape paper. Dirty spots reduced by 1% from sprayman’s gloves changing, and 4% from masking tape -changing. Both result are not significant reduction to reach company NG targets. Other improvement sugesstion to be implemented are standarization on facilities and production equipments.
Upaya Penurunan Downtime pada Mesin Moulding di PT. X Marvin Ardyanto; Felecia Felecia
Jurnal Titra Vol 3, No 2 (2015)
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Abstract

PT. X is a company that processed log wood into timber products with size, type of wood, and the shape of the profile are produced depends on the buyer’s order. The company needs the process with a machine that can work continuously without any obstacle in order to meet the demand. Moulding machine in PT. X has downtime with an average 13,22% which the company want to reduce it. The main cause of downtime on the moulding machine is the changeover and breakdown. How to reduce changeover time is by using the method of Single Minute Exchange of Dies (SMED) and reduce frequency and time of the breakdown by making preventive maintenance schedule based on the MTTF value. The proposed improvements to reduce changeover time is doing some activities before the machine stops, making a new storage for tools and ring, and do the parallel changeover. The proposed improvements using the method SMED when applied can reduce changeover time with an average decrease in time estimation of 33,26%. Preventive maintenance schedule on the moulding machines based on the simulation results within a year can reduce downtime due to breakdown with an average of 57,55%.
Perbaikan Manajemen Sistem Gudang di PT. Dewata Cipta Semesta Enrico Tjahjono; Felecia Felecia
Jurnal Titra Vol 3, No 2 (2015)
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Abstract

PT. Dewata Cipta Semesta is a company which focused in sawmills, wood products produced in the form of cut (sawn timber) for building’s materials or furniture’s raw materials. The Warehouse system at the company is still very simple and has many weakness that cause some problems in the company such as the difference between the stock and the physical stock in the warehouse as well as the lenght of the process of unloading. Based on observations and data analysis on company, there are some problems that result in differences in stock and phusical as well as the duration of the process of unloading are: the arrangement of goods in the warehouse are not grouped in detail, two warehouses head leads, and grading process is carried out when loading. Warehouse management system improvement is done to minimize the  difference between the stock and the physical stock in the warehouse as well as accelerate the process of unloading the goods. Warehouse management system improvements made are arrange of the raw material warehouse are grouped by type and diameter of the timber , the warehouse material classified by type , grade and size of the timber , making the Standard Operating Procedure for the warehouse staff. For make the system running properly also proposed to appoint only one head of the warehouse so that there is clarity on the duties and responsibilities of the warehouse. 
Pembuatan Prototipe Hunian Sementara untuk Pengungsi di Indonesia Wilson Edo Santoso; Felecia Felecia; Togar Williater Soaloon Panjaitan
Jurnal Titra Vol 4, No 2 (2016): Jurnal Titra
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Indonesia is a country with highest potential disaster in the world .Some disaster in Indonesia resulted in displaced communities. National Agency for Disaster Management (BNPB) as Indonesian disaster management agency providing emergency shelter for refugees. Problems that arise are refugees have to stay in the emergency shelter for long period of time which should only as an emergency only. This research aims to design a temporary shelter as a bridge between emergency shelters to permanent housing. The design begins with finding the voice of customer (VOC) by way of interviews and news from various media. Results VOC mapped in House of Quality (HOQ) and used as a reference in the design of temporary shelters. Results from this study is the design of temporary shelters and prototype.
Perbaikan Estimasi Loading Bagian Machinery PT. X Mikhael Ariesto Rahardjo; Felecia Felecia
Jurnal Titra Vol 3, No 2 (2015)
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Abstract

PT. X is a industrial machinery company who supply their products to other companies of PT. X parent company. PT. X is currently experiencing major problems in terms of overload capacity and loading estimates are less accurate. This study aims to resolve both of these issues, which can lower the actual loading and improve the accuracy of loading estimation. Repairs carried out by estimating the reduction in loading by reducing the categories of working hours of others. A decrease in working hours of others are able to lower the actual loading is estimated at 24.23% in 2014 and 19.64% in 2015. The real proposal given itself are focus on improvement in the design department. Estimates loading then also carried out after fixing the actual loading conditions. Estimates loading at PT. X itself are having a great error when compared with the actual loading of existing, which amounted to 62.84% in 2014. Improvements loading estimation is done by using optimized manhour quota where uncertainty weight is the most important thing to its result. The resulting error rate amounted to 32.23% for the project loading, 9:48% for the total loading, and 6.78% for the total loading with repairs.
Analisis Available Time pada Mesin A di PT. XYZ Ivan Santosa; Felecia Felecia
Jurnal Titra Vol 5, No 2 (2017): vol 5 no 2, Juli 2017
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Abstract

PT. XYZ is a manufacture company which specializes in producing of car tires, motorcycle tires, truck tires, bus tires, etc. The purpose of this research is to determine the production capacity of machine A and knowing the right solution to maximize the capacity of machine A. Early quality review shows no definite capacity in the production process on a daily basis. Determination of capacity is done by taking data every production process by using stopwatch and conducted a series of data testing. The actual condition of initial production in march was 136 tires/day. The calculation of production capacity was 167 tires / day in March. The analysis of time cycle improvement is done using time motion study method, Man-Machine Chart map, and body ply material improvement on machine A. The result after actual implementation in April was 151 tires / day with capacity of 182 tires/day. The result of analysis shows that the production capacity is known and there is an increase of production capacity by 10% on machine A in PT.XYZ. The factor that makes no chances of catching up is because the percentage of downtime is too big and does not match the target.
Perancangan Tata Letak Fasilitas Pada PT. Lima Jaya Jonathan Wijaya Gunawan; tanti octavia; felecia felecia
Jurnal Titra Vol 3, No 2 (2015)
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Abstract

PT.Lima Jaya is a company that engaged in the field of steel and metalworks. Currently, this company wants to build a new company that specialized in wiremesh production. Therefore, this research tries to design their facility layout for minimizing moment. Three algorithms are applied in order to get the best result. The algorithms are corelap algorithm, aldep algorithm, and blocplan algorithm. The result shows that the blocplan algorithm gives the best result with the moment 13579,4.
Penentuan Spesifikasi Sofa dengan Decision Tree pada Perusahaan X Jonathan Dita Harjadi; Felecia Felecia; Iwan Halim Sahputra
Jurnal Titra Vol 11, No 1 (2023): Jurnal Titra 11(1) Januari 2023
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Company X is a company engaged in the furniture sector. The company has been established since 2003. Company X has a problem, which is that it is still unable to design new product specifications and determine which current products need to be produced again using past demand data. This causes high RnD (Research and Development) cost losses. These costs include drafting costs, costs for making frame molds, fabrics, foam, and prototype costs. With the application of BI to company X, the specifications of the sofa can be found out according to the interests and needs of consumers. The data used in this study are sales from January 1, 2021 to June 30, 2022. The method used to conduct this research is the decision tree version ID3 and C4.5. After being tested using cross-validation 10 times, the results of the accuracy show that the C4.5 version of the decision tree is more accurate than the ID3 version. The results of this study are to determine the sofa specifications that customers are interested in based on price segmentation. Categories based on price are divided into 3, namely PR3, PR2, and PR1. There are 6 significant sofa specifications in PR2. There are 3 significant sofa specifications in the PR3.
Peningkatan Value Added Activity Refiller Warehouse Lantai 2 di PT. Schneider Electrics Manufacturing Batam (SEMB) Michael Joseph Konstantinus; Felecia Felecia
Jurnal Titra Vol 11, No 2 (2023): Jurnal Titra 11(2) Juli 2023
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Abstract

PT. Schneider Manufacturing Batam has high NPV cost data. NPV or non-proportional to volume, namely costs that do not provide direct added value to the product. This is shown from the data on storage hours in the 2022 period which is still a negative number with an average of -1776.83 hours/month. The condition that occurs in the field is that refillers often carry out activities that should not be important. With the current condition of the warehouse there are three operators, this number can still be reduced. This operator reduction will have an impact on reducing production costs. The method used in this research is DMAIC. Analysis using motion studies on the activities of the fillers is then classified as value-adding or non-value-adding activities. The initial average value added using the three refillers was 47% and increased by 74%, it was seen that there was an increase of 27%. The reduction in refiller operators has had a positive impact and refill operators can still work on all job desks with only two operators.