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Journal : Vortex

RELIABILITY LEVEL ON AFCS ACTUATOR COMPONENT OF THE SIKORSKY S-76 HELICOPTER Aryanti Dwi Puspita; Sri Mulyani; Karseno KS
Vortex Vol 1, No 1 (2020)
Publisher : Institut Teknologi Dirgantara Adisutjipto

Show Abstract | Download Original | Original Source | Check in Google Scholar | Full PDF (504.629 KB) | DOI: 10.28989/vortex.v1i1.716

Abstract

The use of helicopters is very useful for Indonesia's natural conditions which is in the form of islands. In order to support the helicopter's capabilities, an AFCS actuator or automatic flight control system actuator is needed to make the flight automatically. Therefore, the author tries to conduct a reliability analysis to determine the level of reliability of the AFCS Actuator component in S-76 helicopter. The method used to conduct the analysis is the Weibull distribution method, which is one of several methods that are often used. The main objective is to determine the level of reliability and characteristics of the failure modes that often occur in these components. By analyzing at the results of calculations and types of failures, it can be seen the types of effective treatments to be applied to the AFCS Actuator component.
Manufacturing Engine Test Bed Dle-55cc Single Cylinder Petrol Siti Iin Infitah Hilmiah; Sri Mulyani; Lazuardy Rahendra P
Vortex Vol 2, No 2 (2021)
Publisher : Institut Teknologi Dirgantara Adisutjipto

Show Abstract | Download Original | Original Source | Check in Google Scholar | Full PDF (481.423 KB) | DOI: 10.28989/vortex.v2i2.1007

Abstract

The engine test bed is a tool used for testing in the development of new aircraft when it is installed into the aircraft to determine the capabilities of each engine. This engine test bed research aims to meet the needs of the learning process in supporting the practicum. By determining the geometry, modeling, material selection, manufacture, and testing of the engine test bed it will be known that the engine performance is good before use. The method used is a practical and analytical method to analyze the data that has been obtained from the test. The object of research used in this study is a dle-55cc engine. based on the results of testing the results of the thrust that compares with the static value of the thrust calculator, the average difference is obtained. From the results of the comparison of errors on the test equipment, the 22×8 propeller (4.5cm chord) obtained an average error of 4.178%. While the propeller 22×8 (chord 5cm) the error generated is 3.719% and from the value of fuel consumption obtained it produces 588,600-20,708 (N/kW.hr) this shows a good level of decline, so the engine used is more efficient in its use. From the test results, it can be said that the engine test bed has accuracy and can produce good engine performance to be used as a testing and other learning tool.