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ULASAN TEKNOLOGI PRETREATMENT TERKINI LIMBAH CAIR POME SEBAGAI UMPAN DIGESTER BIOGAS Murti, Galuh Wirama; Pertiwi, Astri; Masfuri, Imron; Juwita, Asmi Rima; Adiprabowo, Arya Bhaskara; Dwimansyah, Ridho; Senda, Semuel Pati; Prasetyo, Dwi Husodo
JTERA (Jurnal Teknologi Rekayasa) Vol 4, No 1: June 2019
Publisher : Politeknik Sukabumi

Show Abstract | Download Original | Original Source | Check in Google Scholar | Full PDF (958.298 KB) | DOI: 10.31544/jtera.v4.i1.2019.17-28

Abstract

Pengolahan anaerob merupakan teknologi efektif yang murah untuk mengolah limbah cair kelapa sawit (POME) menjadi biogas yang dapat dijadikan bahan bakar atau listrik. Yield biogas dapat ditingkatkan dengan menerapkan teknik pretreatment limbah POME sebelum menuju digester. Umumnya, teknik pretreatment ini adalah tahapan hidrolisis yang merupakan tahap pertama dari produksi biogas. Tujuan dari pretreatment ini untuk memecah padatan atau gumpalan komponen agar lebih mudah dicerna oleh bakteri. Studi ini berisi ulasan perbandingan keunggulan dan kelemahan beberapa metode pretreatment terkini termasuk dengan evaluasi biaya operasional yang sesuai untuk diaplikasikan pada pengolahan pretreatment limbah POME di PKS Sei Pagar. Berdasarkan hasil seleksi, teknik pretreatment dengan karakteristik limbah POME yang memiliki biaya operasional relatif rendah yaitu teknik ultrasonik dan ozonasi.
APPLICATION OF INSTRUMENTATION AND CONTROL SYSTEM FOR BIOGAS POWER GENERATION COMMISSIONING AT PTPN V KAMPAR PALM OIL MILL Salehah, Nur Azimah; Prasetyo, Dwi Husodo; Senda, Semuel Pati; Supriyadi, Muhamad Rodhi; Adeliaa, Nesha; Samodra, Bayu; Adiprabowo, Arya Bhaskara; Muharto, Bambang; Anindita, Hana Nabila
Majalah Ilmiah Pengkajian Industri Vol 14, No 1 (2020): Majalah Ilmiah Pengkajian Industri
Publisher : BPPT

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.29122/mipi.v14i1.3865

Abstract

Biogas Power Plant (PLT) from palm oil mill effluent had been commissioned by a team from the Center of Technology for the Energy Resources and Chemical Industry, Agency for the Assessment and Application of Technology (PTSEIK-BPPT). The biogas power plant is located in PTPN V Kampar, Riau Province. A PLC (Programmable Logic Controller) has been implemented to support the operation of biogas power plant. Proper sensor selection has been done for each measurement applications. A computer and mimic panel is used as an interface for the operation of PLC. The master control system communicates with the slave control systems and Human Machine Interface (HMI) by means of ethernet communication protocol. Commissioning phase is carried out for 2 hours with a load of 450 kW. Instrumentation and control system is able to measure important variables such as fluctuation in methane numbers, pressures, and biogas flow rate to check the suitability of biogas supply in accordance to gas engine specification.
APPLICATION OF TEMPERATURE CONTROL SYSTEMS AT THE CATALYST ACTIVATION STEP IN THE METHANOL TESTPLANT Adiprabowo, Arya Bhaskara; Pertiwi, Astri; Rahmawati, Nurdiah; Saputro, Frendy Rian; Valentino, Novio; Anindita, Hana Nabila; Septriana, Desy
Majalah Ilmiah Pengkajian Industri Vol. 15 No. 1 (2021): Majalah Ilmiah Pengkajian Industri
Publisher : Deputi TIRBR-BPPT

Show Abstract | Download Original | Original Source | Check in Google Scholar

Abstract

Catalyst activation is an important step in methanol synthesis process, achieved by the reduction of CuO precursor producing Cu0 active sites.  Testplant’s temperature operation shall be maintainted at 220°C in order to maximize the CuO reduction process in the catalyst activation step. A temperature control system shall be applied in methanol testplant to maintain the temperature during reduction process, due to sensitivity of reduction process to temperature variation and possibility of disturbance such as change in gas flow rate which could affects the operating temperature. Temperature control systems are tested by using step response at the desired setpoint, which is 220°C at pre-heater and reactor and 60°C at sampling line. The tests are conducted by changing the setpoint value at temperature controller and previously stable flow gas in the system (disturbance rejection). The temperature control system proved to be able to response well during the test. In the end, methanol is produced from syngas, indicating catalyst activation success. Keywords: Catalyst Activation; Methanol Testplant; Temperature Controller
Pyrolysis process control: temperature control design and application for optimum process operation Muharto, Bambang; Saputro, Frendy Rian; Prabowo, Wargiantoro; Anggoro, Trisno; Adiprabowo, Arya Bhaskara; Masfuri, Imron; Irawan, Bagus Bhakti
International Journal of Electrical and Computer Engineering (IJECE) Vol 14, No 2: April 2024
Publisher : Institute of Advanced Engineering and Science

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.11591/ijece.v14i2.pp1473-1485

Abstract

Fast pyrolysis in auger reactor gains attention for efficient bio-oil production. Due to the quick nature of the process, precise temperature control using the proportional-integral-derivative (PID) algorithm is paramount. This study harnesses various PID tuning approaches through modelling and experimental validation to optimize continuous and precise pyrolysis temperature. System identification was done to investigate the process dynamic with fit accuracy above 93% and design a suitable PID control. Comparison with the experiment data shows a favorable result with rise time and settling time match above 75%. Ziegler-Nichols (ZN) and Cohen-Coon (CC) tuning methods were implemented in the system with undistinguished results, yielding steady-state error (SSE) below 1% and settling time around 4,300 to 4,800 seconds. The heuristic fine-tuning method improved the rise time and settling time by stabilizing before 3,600 seconds. Furthermore, the robustness of PID controllers was verified with a disturbance rejection test, keeping the SSE deviation inside the boundary of 2%. Finally, the setup could support maximum pyrolytic oil production by 69.6% at 500 °C. The result implies that the PID controller could provide a stable and rugged response to support a productive and sustainable pyrolysis plant operation.