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Redesain Dies Proses Blank-Pierce dengan Penyesuaian Mesin Press Guna Meningkatkan Efisiensi Produk Reinforcement Quarter Panel Extension RH/L Desy Agustin; Ibnu Syihab; Sanurya Putri Purbaningrum; Abdul Wahid Arohman; Indra Rizki Pratama
Jurnal Serambi Engineering Vol. 9 No. 2 (2024): April 2024
Publisher : Faculty of Engineering, Universitas Serambi Mekkah

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Abstract

The redesign of the die design in the blank-pierce process for the RH/LH quarter panel extension reinforcement product was carried out using field observations to obtain actual data. The production process consists of five stages: blanking, piercing, restriking, bending and forming. Meanwhile, in the redesign process, the RH/LH quarter panel extension reinforcement product is evaluated in the blanking and piercing die processes. Cycle time analysis after the tool design has been redesigned shows the potential for increasing efficiency by reducing process time. MPP data is used as a guide for die design with relevant machine specifications, die size and materials. Machine pressure and tonnage calculations were carried out for the current die design and the revised version, showing significant improvements in production efficiency. The die redesign was carried out to increase output per stroke and to use more sophisticated automation processes. The results of this research show that improved die design can increase production efficiency and productivity by reducing the number of strokes required and properly adjusting machine capacity.
Implementasi Jig Welding Untuk Meningkatkan Efisiensi Pengelasan Frame Base Purbaningrum, Sanurya Putri; Johannes, Johannes; Imansuri, Febriza; Salati, Dianasanti; Solih, Edwin Sahrial
Journal of Community Services in Sustainability Vol. 2 No. 1 (2024): Journal of Community Services in Sustainability
Publisher : Politeknik STMI Jakarta

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.52330/jocss.v2i1.277

Abstract

Pengelasan adalah proses penting dalam pembuatan komponen logam, termasuk base frame, yang membutuhkan presisi dan efisiensi tinggi. Namun, proses pengelasan manual sering kali menghadapi masalah ketidakstabilan dan ketidakkonsistenan hasil. PkM ini bertujuan untuk mengimplementasikan jig welding dalam proses pengelasan base frame guna meningkatkan efisiensi dan kualitas hasil pengelasan. Jig welding dirancang untuk menahan dan menempatkan material dengan presisi, mengurangi waktu penataan, serta meminimalkan kesalahan manusia. Melalui penggunaan jig welding, diharapkan dapat terjadi peningkatan signifikan dalam efisiensi waktu dan pengurangan biaya produksi, sekaligus meningkatkan keselamatan kerja. Hasil penelitian menunjukkan bahwa implementasi jig welding dapat meningkatkan kecepatan proses pengelasan hingga 80%, mengurangi cacat pengelasan, dan memperbaiki kualitas
Application of Single Minute Exchange Die (SMED) Method to Minimize Setup Time on 350T Capacity Molding Machine Sumasto, Fredy; Arrofah, Muhammad Arif; Pratama, Indra Rizki; Purbaningrum, Sanurya Putri; Satria, Adam; Rapi, Amrin
Jurnal Inotera Vol. 10 No. 1 (2025): January-June 2025
Publisher : LPPM Politeknik Aceh Selatan

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.31572/inotera.Vol10.Iss1.2025.ID422

Abstract

This study aims to apply the Single Minute Exchange of Die (SMED) method in reducing setup time on a 350T capacity molding machine at PT HMG. The data collection results showed that the frequency of mold changes reached 70 times a month, with the average time required for mold changes before the implementation of SMED 173 minutes. After the implementation of SMED, the mold change time was successfully reduced to 64 minutes, reflecting a decrease of 63%. The implementation of SMED was carried out through several stages, including converting internal activities to external ones, which aimed to reduce machine downtime. Optimization of the remaining activities was also carried out, such as reducing the temperature drop time on the barrel and hot runner, which previously took 15 minutes, now only 5 minutes. The final results showed that machine downtime cost savings reached Rp11,200,000 per month after the implementation of SMED, with total downtime costs decreasing from Rp30,274,999 to Rp19,074,999 per month. This study proves that implementing the SMED method can significantly improve time efficiency, reduce production costs, and create more efficient operational standards. The findings provide a solid basis for further development in industry manufacturing practices.
Rancang Bangun dan Analisis Jig Welding Pengelasan Siku Sebagai Alat Bantu Praktikum Produksi Jig & Fixture di Politeknik STMI Jakarta Nurhadi, Fadhil Fadhlurrohman; Purbaningrum, Sanurya Putri; Solih, Edwin Sahrial; Rifai, Ahmad; Al Fatir, Aditya; Yudhistira, Hilmi; Satriatama, Adrian
Jurnal Serambi Engineering Vol. 10 No. 2 (2025): April 2025
Publisher : Faculty of Engineering, Universitas Serambi Mekkah

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Abstract

Angular welding is a commonly utilized technique in the manufacturing industry, particularly in the construction of frame structures. The primary challenge in angular welding is ensuring the accuracy of the angles and the strength of the joints. At Polytechnic STMI Jakarta, the Jig & Fixture Production course aims to train students in using appropriate manufacturing techniques and tools, including welding jigs. The use of welding jigs can improve the precision, efficiency, and consistency of welding results, while also reducing the risk of human error. This study aims to design and analyze a welding jig for angular welding in the context of practical coursework at STMI Jakarta Polytechnic. The research methodology includes a literature review, jig design using CAD software, prototype development, and performance testing and analysis of the welding jig. The expected outcomes of the study are to enhance the quality and efficiency of the angular welding process. Additionally, the designed welding jig provides ease of use for students, thereby reducing errors caused by human factors.
CLAMPING DIES DESIGN TO MINIMIZE AUTOMOTIVE COMPONENT DIES SETUP TIME AT PT GANDING TOOLSINDO Purbaningrum, Sanurya Putri; Lianny, Indah Kurnia Mahasih; Solih, Edwin Sahrial; Arohman, Abdul Wahid; Satiman , Bayu
Media Mesin: Majalah Teknik Mesin Vol. 25 No. 2 (2024)
Publisher : Universitas Muhammadiyah Surakarta

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.23917/mesin.v25i2.3012

Abstract

PT Ganding Toolsindo was faced with the problem of high automotive component die setup times. The main cause of the high setup time is the process of tightening and releasing the bolts which is done manually. The aim of this research is to design a tool for clamping dies which functions to help speed up the bolt installation process, so that the setup time for automotive component dies is reduced. The method used in this research is field observation followed by the die clamping design process. Design planning begins by drawing the object using CAD software based on the results of load calculations and determining the dimensions of the dies themselves and the press machine as well as selecting the dies material. Furthermore, proof was carried out that this die clamping design could reduce dies setup time using movement analysis with a pre-determined time study Measurement Time Method (MTM) method, where the results showed a time saving of 92.4%.
Penerapan Single Minute Exchange of Dies (SMED) untuk Optimalisasi Proses Pergantian Dies pada Mesin Press SEYI SN2-300 di PT Ganding Toolsindo Purbaningrum, Sanurya Putri; Solih, Edwin Sahrial; Lianny, Indah Kurnia Mahasih; Satiman, Bayu
Journal of Community Services in Sustainability Vol. 3 No. 1 (2025): Journal of Community Services in Sustainability (April 2025)
Publisher : Politeknik STMI Jakarta

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.52330/jocss.v3i1.373

Abstract

Penerapan metode Single Minute Exchange of Dies (SMED) pada mesin press SEYI SN2-300 di PT Ganding Toolsindo bertujuan meningkatkan efisiensi pergantian dies dalam produksi. Tahapan program mencakup analisis proses, sosialisasi, pelatihan, pendampingan, serta evaluasi penerapan SMED. Implementasi menghadapi kendala pada identifikasi aktivitas internal dan eksternal serta adaptasi teknisi terhadap metode baru. Dengan analisis dan pelatihan intensif, beberapa aktivitas internal setup berhasil diubah menjadi eksternal, sehingga waktu setup turun menjadi 29,58 menit dari sebelumnya 35,73 menit. Selain mengurangi downtime, SMED mendukung sistem operasional yang lebih terstruktur, meningkatkan standar kerja, dan kualitas produksi. Evaluasi menunjukkan efektivitas SMED dapat terus ditingkatkan dengan alat bantu tambahan. Implementasi ini tidak hanya meningkatkan efisiensi, tetapi juga membangun budaya kerja disiplin dan berkelanjutan yang mendukung efisiensi waktu, pengurangan biaya, dan peningkatan kualitas produksi.
Reduction Cost in Endplate-B Material Component for Oil Filter Bypass System with Redesigning Satria, Adam; Sahrial Solih, Edwin; Putri Purbaningrum, Sanurya; Wahid Arohman, Abdul; Ridho Hans Gurning
Jurnal Serambi Engineering Vol. 10 No. 3 (2025): Juli 2025
Publisher : Faculty of Engineering, Universitas Serambi Mekkah

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Abstract

The bypass system in spin-on type oil filters plays a crucial role in maintaining engine cleanliness and performance by allowing oil to flow when excessive pressure occurs. A critical component of this system is endplate-B, which fulfills dual roles: providing structural support and functioning as an interface for oil passage during bypass operations. However, the relatively high material usage and cost associated with the current design of endplate-B pose challenges in manufacturing efficiency. The objective of this study is to minimize the material cost of endplate-B by optimizing its dimensional geometry without compromising its structural and functional performance. The research methodology encompasses dimensional redesign, structural analysis, and performance validation under simulated operating conditions. The findings indicate that strategic dimensional modifications can substantially reduce material usage while preserving mechanical strength and functional integrity. The implementation of this optimized design provides a cost-effective solution for the manufacturing of oil filters and contributes to broader efforts to improve production efficiency in the automotive component industry.