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Contact Name
Riki Ruli A. Siregar
Contact Email
riki.ruli@sttpln.ac.id
Phone
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Journal Mail Official
riki.ruli@sttpln.ac.id
Editorial Address
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Location
Kota adm. jakarta barat,
Dki jakarta
INDONESIA
Power Plant
ISSN : 23561513     EISSN : 2656372X     DOI : -
The Scientific Journal of "Power Plant" is a collection of scientific works by lecturers, researchers, and practitioners in the field of Mechanical Engineering that have been published since September 2012. This journal is the result of scientific work, research in the fields of Energy, Materials and Energy Conversion to contribute in writing scientific which will be useful for the application of science and technology, especially in the field of Mechanical Engineering.
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Articles 10 Documents
Search results for , issue "Vol 2 No 2 (2014): JURNAL POWER PLANT" : 10 Documents clear
Redesign Line Drain Pada Filter Heat Exchanger PLTU Indramayu Andika Widya P; Mae Nitto Budi Karsono
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.803

Abstract

The use of electricity in modern life today is a necessity and demands that can not be separated from everyday activities. Indramayu power plant which has a capacity of 3 x 330 MW is one of the coal-fired thermal power plant that supplies the system interconnect JAMALI (Java, Madura, Bali). Thus generating performance reliability is a must. In the production process kapaitas Indramayu with 3 x 300 MW, there are many tools that support to optimize the power production process, whether it is the main equipment and auxiliary equipment. The main equipment at this plant, among others such as boilers, turbines, generators and condensers. Indramayu contained cooling water cycle that serves to cool the various systems, for example: as a generator coolant, lube oil coolers, etc. In the cooling water cycle, there are a medium for transferring heat from a hot medium into a cold media, the tool is called Heat Exchanger (HE) .Heat discussed exchanger using sea water cooling medium, so it is prone to dirty / clogged. Therefore, before entering the heat exchanger there is a filter called debris filter Heat Exchanger. In pengoprasian debris filter Heat Exchanger there are many obstacles, one of which is the overflow of water in the sump tank which would cause flooding on the ground floor and the matter will be discussed in this project so that it does not reoccur.
Analisa Dampak Penambahan Line Flushing Injeksi Phosphate Arief Suardi Nur Chairat; Moch Zainal Arifin
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.805

Abstract

Condensate water is the main ingredient in the process of generating steam in the power plant condensate water uap. Therefore must have a good quality so it does not cause damage to the equipment - equipment such as pipes, tubes, valves and others. To produce water quality condensate desirable it is necessary chemicals include phosphate, ammonia and chemical hydrasin. Material is injected into some equipment such as deaerator, steam drums and others. On this occasion the discussion is about the injection of chemicals phospat. Material the chemicals injected into the water condensate (feed water) which will be precisely in the boiler to the steam injection process takes drum. For pump chemicals from the tank in order to get to the steam drum. Therefore the pump and the output pipe leading the steam drum to be reliable so it does not interfere with the injection process resulting in the boiler water quality does not match the prescribed standards that disrupts the production of listrik.Namun on the way there has been a disruption especially at pipe outlet (discharge line) to the steam drum is clogged (plugging) .This occurs because after the injection process there are still remaining - the rest of phosphate in the pump, pipe valve outlet and then dries and crystallizes as kapur.This happens especially when the power is turned off for a long time (over houl). From the above problems it is necessary to add the channel for flushing (flushing) on ​​the pump and the discharge channel leading to the steam drum, especially when the power will be off for a long time so there is no plugging in the pipe leading to the pump outlet steam line drum. The addition of the plumbing connected condensate (from discharge CEP) to the pump inlet pipe phosphate.
Kajian Modifikasi Sistem Udara Instrumen Untuk Peningkatan Kehandalan PLTU Indramayu Eko Sulistyo; Indah Handayasari; Nur Rohman Aziz
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.808

Abstract

Reliable power generation can not be separated from the reliability of the power plant system integration. At the power plant, in particular all the power plant system reliability must be maintained so that no damage is fatal. Especially the instrument air system which is driving tools instrumentation. At indramayu power plant with an installed capacity of 3 x 330 MW nearly all settings instrumentation equipment sourced from compressed instrument air. This system is derived from the rotary screw compressor manifold floaded oil. In the instrument air system contained additional equipment to maintain the quality of the air produced is water dryer. But the fact of compressed instrument air quality is not good and still below the standards of ANSI / ISA-S7.0.01-1996. The output pressure of the compressed air system is also less. Normal operating pressure is 0.75 - 0.8 Mpa, but in actual field conditions of water stress on the receiver tank just 0:57 -0.64 MPa. This happens because of the existing compressor 5 only 3 that stand by. The performance of the compressor that is running downhill. It can be seen from the resulting pressure dropped from 0.85 MPa to 0.76 MPa. Based on these problems required the study and modification of compressed instrument air supply to find the best solution.
Analisis Tegangan Untuk Setiap Kapasitas Belt Conveyor C4 PLTU Indramayu 3 X 330 Mw Ammar Asof; Nurmiati Pasra; Ulil Absor
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.810

Abstract

Belt conveyor is a device used to transfer coal combustion chamber (furnice) in Steam Power (power plant). In the Indramayu power plant conveyor conditions in the field often occurs over tracking the conveyor belt and the belt results in the termination of coal burning. A voltage that is too large will cause the working of the belt conveyor to be heavy so that it can lead to broken shaft and idler pulley. While the voltage is too small to make the cause of the conveyor belt out of the track resulting in slippage into the pulley. The voltage on the conveyor belt must be known with certainty to prevent failed operations on the conveyor. In this case penlis will analyze the voltage for each operating capacity of belt conveyor C4 using the standard CEMA (Conveyor Equipment Manufacturers Association) 6th Edition, 2002. So with the proper voltage, the operation of conveyor C4 can walk normally.
Analisis Kerugian Out Service High Pressure Heater No.7 Pada PLTU Paiton Unit 2 Harun Al Rosyid; Wahyu Alghifar Pusipto
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.812

Abstract

Operation of Steam Power (power plant) is highly dependent on the thermal efficiency as a reliability parameter unit. PJB is required to operate and maintain the power plants with world-class quality standards, and is able to maintain the efficiency of the work unit to keep it in optimum condition. In this study used a method in which the actions of this method has the objective to develop the skills, checking, analysis and influence the fuel consumption of the primary to the efficiency of Paiton # 2 due to the application of the inspection work at high pressure heater is no.7.The goal of operate back HPH 7 performance optimal, and calculate the rate of heat transfer coefficient on the concession system.
Rancang Bangun Boltheater Electric Dengan Sistem Pengendali Berbasis SMS Controller Untuk Bongkar Pasang Baut Casing Dan Valve Turbin Jasmid Edy; Retno Aita Diantari; Arman Susanto
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.814

Abstract

The steam turbine generator is the main equipment working at high temperature and pressure so it is very important to do regular maintenance to guarantee keandalannya.Pemliharaan is a simple routine inspection, inspection mean and serious inspection. Serious when turbine maintenance inspection (demolition total) there tubin demolition work and the valve casing turbine in penangananya requires a special instrument called boltheater. The tool is a tool for the disassembly bolt turbine casing and turbine valve with the principle of heating the bolt, causing expansion and further used for disassembling the bolt. Mertode previous boltheater operation is manually which has several shortcomings kekurangan. So to avoid the need for a remote control and one of them is a remote control system based on SMS controller. Automatic control has the advantage of efficient use of personnel which impact on the efficiency of maintenance costs, speed up the process of work (time efficiency) and reduce the risk of workplace accidents during the process of disassembly turbine casing and turbine valve. The existence of the efficiency of the time when the overhaul will increase the chance of generating units operate. Opportunity for all operating units of the plant affects the value of EAF (Equivalent Availability Factor). This is a measure of the success of a plant in the supply and sell electricity.
Penerapan Metode Chemical Cleaning Guna Meningkatkan Kualitas Produk SWRO Pada Sistem Reverse Osmosis PLTGU Tambak Lorok Prayudi Prayudi; David Ariyanto
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.816

Abstract

Reverse Osmosis systems at Pond PLTGU Lorok is a system that has the principle of using a micro filtration membrane. Applying the theory behind the osmotic pressure which will be filtered sea water into fresh water. Reverse Osmosis system in the absence of biocide chemical injection system which serves to prevent the formation of organic fouling in membrane. In the SWRO system using a feedwater in the form of sea water where a lot of particulate matter contained therein. If the particulate escaped from pretreatment system will be able to clog the membrane. So that the flow rate will reduce the yield of the product as well as increase the value of the product konduktivity SWRO. In order to improve its quality, it is necessary to dissolve Chemical Cleaning foulant attached to the membrane. From the results of the Chemical Cleaning has been done then obtained an increase in the flow of products SWRO of 27 liters / minute.
Analisa Gangguan Failure To Ignite Pada GTG 1.3 Tambak Lorok Dengan Metode RCFA Roswati Nurhasanah; Gita Puspa Artiani; Gaguk Sujadmiko
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.818

Abstract

PLTGU designed for continuous running, but because of the condition of the network then UP Semarang is conditioned only operate during peak hours or when required by the Dispatcher because other units are holding maintenance or because of something that can not operate. This condition makes the gas turbine units at UP.Semarang often operate with a pattern start / stop, so that the equipment plays an important role in the process of start / stop required for work excellence. The method used to analyze the root cause failure disorders to Ignite Gas Turbine is the method of Root Cause Failure Analysis (RCFA). Based on the results of analysis by method RCFA, disruptions caused by failure to Ignite Liquid Fuel Nozzle Check Valve Failure to obtain Task that is in addition to the regular maintenance schedule after GTG operated by MFO also implement new PM replacement check valve for no.1 to 14 every 6 months , manufacture PM Visual check every 1 week and the addition of a new Prime Minister for a replacement check valve No. 4,5,10,11,13 and 14 every 3 months because often damaged.
Peningkatan Daya Mampu Dan Efisiensi PLTG Tipe ABB 13E2 Melalui Optimalisasi Sudut VIGV Sahlan Sahlan; Erlina Erlina; Ronny Koeshartarto
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.820

Abstract

Gilimanuk power plant (ABB 13E2) with an installed capacity of 133.8 MW generating units that have a strategic role in the Bali Sub Systems (± 25 % when the Peak Load) . A decrease in power capable , increased heat rate , especially when approaching the maintenance period , becomes a problem that impact on the efficiency of the unit . Departing from the problem arose the idea that by optimizing the angle openings VIGV (Variable Inlet Guide Vane) but remains within safe limits with the aim of improving the performance and efficiency of the generating units. After optimization of the opening angle of VIGV gained increased power capable of 2-3 MW units , an increase of 0.2 % efficiency units and no adverse effect on the material and exhaust emissions after the NDT test in 2012 Major Inspection and monitoring of emissions via CEMS .
Analisa Pengaruh Cleaning Kondensor Terhadap Vibrasi CWP 2C Vakum Kondensor Dan Temperatur Cooling PLTU Paiton 2 Vendy Antono; Dika Wahyu Wijaya
JURNAL POWERPLANT Vol 2 No 2 (2014): JURNAL POWER PLANT
Publisher : Sekolah Tinggi Teknik - PLN

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.33322/powerplant.v2i2.822

Abstract

In the process of production of the power plant cooling water system has a very important role to change the vapor phase from the expansion turbine into water stored in Hotwell. The condenser is equipment which becomes the venue for the process, but keep in mind the level of cleanliness of the condenser becomes an important factor because it can reduce the heat transfer in the condenser and reduces the cooling process. Moreover, it can also result in other equipment eg in CWP (circulating water pump) increased vibration due to flow of pumped water can not flow the maximum because of blockage in the tube-tube condenser can for garbage, excrement of marine life, or the rubber peeled off later cover tube-tube condenser. This will also result in the efficiency of the unit as well as derating occurs during the process of cleaning the condenser. Cleaning the condenser lowers vibration values ​​CWP 2C Motor inboard side Axial from 6754 mm / s to 1080 mm / s and horizontal outboard motor side of 4645 mm / s to 2827 mm / s according to ISO 10816-3 standard vibration value falls within the normal conditions of operation .Kenaikan dry vacuum condenser before becoming 695 mmHg 683 mmHg after cleaning the condenser this is because the maximum heat transfer process. Mass amounts of water cooling which increased from 15133.88 kg / s into 19221.1 kg / s cause the temperature difference cooling water in and out decreased from before cleaning the condenser is 13 0C becomes 8.6 0C.

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