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Journal : Vortex

Penanganan Vibration Propeller menggunakan Metode Fault Tree Analysis pesawat KT-IB Woong Bee Kurniawan, Riski; Pamungkas, Sunu Aditya; Prakoso, Agung; Lukito, Indro; Budiono, Cyrilus Sukaca; Soemarwoto, Wahyudi
Vortex Vol 5, No 2 (2024)
Publisher : Institut Teknologi Dirgantara Adisutjipto

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.28989/vortex.v5i2.2418

Abstract

Propeller yang diputar oleh engine dapat menghasilkan gaya dorong, karena bentuk blade propeller sendiri yang menyerupai airfoil pada wing pesawat jika dilihat dari penampangnya. Pada pesawat KT-1B Woong Bee, propeller yang digunakan adalah HC-E4N-2/E9512CB-1, jenis adjustable pitch dengan 4 blade. Agar propeller berfungsi optimal, putaran harus stabil untuk memastikan gaya dorong dan kenyamanan penerbangan. Vibration pada propeller sering disebabkan oleh ketidakseimbangan blade, yang bisa terjadi akibat perbedaan berat blade atau perbedaan angle of attack. Analisis kegagalan vibration propeller dilakukan dengan observasi dan data kegagalan dari pesawat KT-1B Woong Bee dalam tiga tahun terakhir (2021-2023). Data tersebut dianalisis menggunakan metode Fault Tree Analysis (FTA) untuk menemukan basic event vibration yang kemudian dianalisa kembali untuk menentukan modus kegagalan yang berupa different weight pada blade yang kemudian dilakukan penanganan berupa balancing propeller, yang mencakup penambahan beban pada blade untuk menyeimbangkan berat blade propeller.
CASE ANALYSIS ON FLIGHT CONTROL SYSTEM SIKORSKY S76 C++ FAILURE FROM YAW CONTROL ASPECT Rahmawati, Fajar Khanif; Lukito, Indro; Baihaqi, M Imam
Vortex Vol 3, No 1 (2022)
Publisher : Institut Teknologi Dirgantara Adisutjipto

Show Abstract | Download Original | Original Source | Check in Google Scholar | Full PDF (495.451 KB) | DOI: 10.28989/vortex.v3i1.1155

Abstract

Flight Control is a system that functions as a helicopter control center. Failure that occurs in flight control would certainly result inconvenience of the pilot in operating the helicopter, even the movement of the helicopter can out of control causing incident or accident. The continuity of the helicopter operation is affected by the maintenance system applied. One of mode moving system helicopter is yaw control, that could control the nose helicopter to move right and left. Fault Tree Diagram could described  analytical technique, whereby an undesired state of the system is specified (usually a state that is critical from a safety or reliability standpoint). The system then analyzed in the context of its environment and operation to find the solution. Based on the analysis results of failures that occurred in the Sikorsky S76 C ++ helicopter flight control from yaw control aspect in the period of January 2015 to May 2018 with an average use of helicopter’s 2092.05 flight hours, there were 46 failures which caused by yaw control. Based on diagram, there were 4 basic events which caused unschedule maintenance on Sikorsky S76 C ++ helicopter flight control system because of yaw fail control,  so that a replacement or repair was needed for the components that affected to the system failure.