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Articles 949 Documents
Reliability centered maintenance menggunakan pendekatan fuzzy logic veronica -; Felecia -; Siana Halim
Jurnal Titra Vol 1, No 1 (2013)
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Abstract

Reliability centered maintenance adalah suatu metode yang digunakan untuk menen­tukan apa yang harus dilakukan supaya aset fisik yang di­miliki dapat tetap terus diguna­kan. Peng­olahan metode reliability centered maintenance membutuhkan jawaban responden se­ba­gai sum­ber utama. Jawaban responden yang tidak selalu dapat mutlak ‘ya’ dan ‘tidak’ me­nyebabkan adanya ketidak pastian. Metode fuzzy akan menghilangkan ketidakpastian dengan mem­­­berikan kebenaran secara gradasi sehingga jawaban responden dapat digunakan didalam me­­tode reliability centered maintenance. Data dan jawaban dari bagian pemeliharaan mengenai komponen mesin yang meng­alami ke­gagalan akan diproses menggunakan kedua metode (reliability centered maintenance dan fuzzy lo­gic) sehingga dapat ditentukan jenis pemeliharaan. Hasil jenis pe­meliharaan metode RCM meng­gunakan pendekatan fuzzy logic lebih efektif dan tepat da­lam mendeteksi jenis pe­meliha­ra­an bagi mesin perusahaan.
Perancangan Sistem Analisa Regulasi di Departemen Customs and Excise Compliance pada PT X Aulastine Setiawan; Karina Agustin
Jurnal Titra Vol 7, No 2 (2019): Jurnal Titra
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Abstract

PT X is a multinational company which has a lot of markets overseas. This international market triggered PT X to do the export and import activity. Export and import at PT X is handled by Customs and Excise Department with Compliance as one of its sub department. One of Compliance’s tasks and functions are analyze a regulation and socialize it to the stakeholders. There are a lot of regulations that regulate about export and import and the regulation itself is rapidly changing. This things cause Compliance Department a delay in analyze and socialize the regulation. The other problem that occur in Compliance Department is they need to know a media that can deliver a regulation effectively. The objectives of this research are designing a system for regulation analysis that can help Compliance Department to do a better keep up with regulation’s changing, to minimize the delay of socialize the regulation, and also to know the right media for socialization. The method that is used in this research to find the most effective media is kruskal-wallis test and SOP is used for designing the system for regulation analysis. The result of data processing shows that the most effective media for socialization is in class training and later, this media will be used for regulation socialization process in SOP.
Perancangan Quality Plan dalam Sistem Manajemen Mutu di sebuah Pabrik Kertas Yonathan Stanley Suryahadi; I Nyoman Sutapa
Jurnal Titra Vol 5, No 2 (2017): vol 5 no 2, Juli 2017
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Abstract

This Paper Company is a manufacturing company at the field of thin paper industry. At the beginning, this company did not have the quality assurance to final product which has the standard of the quality management system. This study represents that the company doesn't have the Quality Plan to the product. The Quality Plan become the main concern to assure the product quality until they are distributed to the customer. This study is meant to design the Quality Plan for the company management system. It will be divided into three parts; first, the inspection of the raw and chemical materials, second, the inspection of the production process, and the final is the inspection of the output jumbo roll. This first inspection is done five times, the second inspection will done in twelve times, and the final process will be done in one process only.
Rancangan Perbaikan Beban Kerja Staf di Departemen Purchasing PT Insera Sena Joan Yuwono; Herry Christian Palit
Jurnal Titra Vol 2, No 1 (2014)
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Abstract

Process of bicycle’s raw materials procurement in PT Insera Sena is handled by Purchasing Department. The problem in the Purchasing Department is employee’s workload at the level of Purchasing head and staff is not balanced. Workload among employees during observation is between 72.56% to 117.46% with average of workload is 97.05%. The evaluation shows that activity performed by Purchasing head and staff are not according to job description and work procedures. Some improvement plans are simulated and workload is between 82.85 % to 99.92 % with average of workload is 92.46 %. These improvement plans can save Rp 10.906.711,11 per year with assumption the minimum wage of Sidoarjo in 2013 is about Rp 1.720.000,00.
Peningkatan Kapasitas Produksi pada UD. X Oliver Wibisono
Jurnal Titra Vol 4, No 1 (2016): Jurnal Titra
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Abstract

UD. X is a crackers factory that currently has a production capacity of 3.6 tons for a day. UD. X wants to increase their production capacity to fullfil their customer’s needs. Production capacity can be increased by improving their steam and packaging process. The drying process is improved by changing the schedule to maximize their production capacity. The packaging process uses time study, therbligs, and right- and left- hand chart to improve the process itself. The drying process is improved by building inventory room for their work in process. The packaging process is improved by introducing two tools which are packaging ring and digital weight scale.The suggestion for steam process increase the production capacity from 3.6 tons to 7.2 tons and the recommendation for packaging process also increase their production capacity from 7.11 ton to 13.36 ton.The suggestion for steam process has been started so the capacity of steam process was increased by 100%. The improvement of packaging process is being applied by adding the operator from 14 to 16 which result higher capacity from 7.11 ton to 8.136 ton  
Identifikasi Penyebab Keterlambatan Pengiriman dan Upaya Penurunan Lead Time Proses pada PT. X Winata Nugraha Saputra
Jurnal Titra Vol 7, No 2 (2019): Jurnal Titra
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Abstract

PT. X is a manufacturing company that produce rigid packaging for cosmetic products. Between January 2018 - March 2019 PT. X got a delivery delay problem up to 391 times, therefore a research was conducted to identify the causes of the delay. This research used root cause analysis as an approach for analyzing the cause of the delay. Delivery delays that had happened in PT. X were caused by actual process lead time (58 days) that took longer than planned process lead time (52 days), therefore creating a gap (6 days). The root cause of the delivery delays are production problems that can be categorized into four type, which is Downtime (39.5%) that caused by mold, machine, process, color, robot, and set up problems; Loss Hour (26.3%) that caused by no norder and preventive maintenance problems; Speed Gap (24.2%) that caused by machine’s actual cavity that are less than the planned cavity and machine’s actual cycle time that took longer than the planned cycle time; Time Reject (10.0%) that caused by black spot, material spot, amandel, appearance, gripis, baret, and mulut tidak pres problems. The potential decrease of the actual lead time when all of the root causes are dealt with are 29.5 days (65.90%)
Upaya Perbaikan Proses Pencatatan Jumlah Barang Hasil Produksi di PT. X Stefen Anthony Binatra; Benedictus Rahardjo
Jurnal Titra Vol 6, No 1 (2018): Jurnal Online Teknik Industri
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Abstract

PT. X is a printing packaging company. This company encounters discrepancy in number of goods produced in a process and affects to the other process. For instance, there are 1000 sheets produced from the beginning of process, but in the next, there are only 800 sheets left. Through observations and interviews, it is found that the problem occurs due to the number of production output is not clearly recorded and the absence of head of department verification. Some suggestions are given, such as making tags at the end of the process at Raw Material Warehouse, positioning reject goods at predetermined place at Offset and Plong Department, and counting the number of rejects in both department. Besides that, acceptance sampling is implemented at Lamination and Glueing Department. In addition, it is also suggested the right method to measure paper in the pallet using measurement tools; the right standard of paper gramatur and work instructions about production order (PO) fulfillment at all departments.
Usulan Penurunan Tingkat Kecacatan Produk Sosis Ayam di PT Charoen Pokphand Indonesia Samuel -; Felecia -
Jurnal Titra Vol 3, No 1 (2015)
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Abstract

PT Charoen Pokphand Indonesia is one of Indonesia’s producer of poultry feed, day old chicks and processed chicken. This research is conducted in sausages plant in Surabaya which produced chicken and beef sausages. Chicken sausages have several types of defects like wrinkled (0,9%), fungus (0,04%), and reject cooking (0,34%). The purpose of this research is to find the defect’s root cause and to propose solutions to reduce chicken sausages defects.DMAIC is used as a method to find problem’s root cause and solution in this research along with interview and direct field observation. It is found that defects caused by operator lack of focus during operation, no quality inspection for PVDC plastic, machine breakdown and no standardized working procedure.This research proposed the company to give morning briefing for operators, quality inspection by quality control department for PVDC plastic, designing tray separator, designing checklist form, downtime form, and work instruction. It is expected to reduced chicken sausages defects up to 1,28%.
PENURUNAN TINGKAT KECACATAN DI PT. MITRA ANUGRAH Stephen Gozali
Jurnal Titra Vol 4, No 2 (2016): Jurnal Titra
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Abstract

This study focuses on the decrease of defects in the critical stage of the production of Kolonel type shoes in PT. Mitra Anugrah. The sewing process and inject process are the most critical process of the production sequence of the shoes. The initial defect rate on the sewing process is 3.35% and on the inject process is 1.22%. The data after implementation shows that the inject process experiences a decrease of defects to 0.97%. On the sewing process, the research is diverted to a sub-contractor by analyzing the percentage of defects in every sub-contractor and making a solution of the problems. Quality plan is only for the critical processes. Daily form and monthly form are made to simplify record keeping in the process of inspecting the sewing sub-contractor. The dimension of the control of the inject process are composisiton and temperature. Dimension of control on the sewing process is the inspection in the sewing department.
Perancangan Modul Verifikasi dan Metode Pemeriksaan Peralatan Produksi Sigaret Kretek Tangan di PT “X” Deisy Ongke; Herry Christian Palit
Jurnal Titra Vol 1, No 2 (2013)
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Abstract

PT “X” is one of the hand-rolled manufacturers cigarettes which using manual process to produce the cigarettes. There were no standardization for verify the production tools. So that every operators could verify those tools in different manners and in fact it caused problems in the production floor. Therefore, a standardization procedures, which is align with the company specification, is an obligatory. As the result of this work, we designed 21 modules for all brands manufactured by PT “X”. Moreover, the study successfully establishes standard procedure, verification form, and verification report which can help maintenance operator to perform production tools verification in every locations.