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Rancang Bangun dan Analisis Jig Welding Pengelasan Siku Sebagai Alat Bantu Praktikum Produksi Jig & Fixture di Politeknik STMI Jakarta Nurhadi, Fadhil Fadhlurrohman; Purbaningrum, Sanurya Putri; Solih, Edwin Sahrial; Rifai, Ahmad; Al Fatir, Aditya; Yudhistira, Hilmi; Satriatama, Adrian
Jurnal Serambi Engineering Vol. 10 No. 2 (2025): April 2025
Publisher : Faculty of Engineering, Universitas Serambi Mekkah

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Abstract

Angular welding is a commonly utilized technique in the manufacturing industry, particularly in the construction of frame structures. The primary challenge in angular welding is ensuring the accuracy of the angles and the strength of the joints. At Polytechnic STMI Jakarta, the Jig & Fixture Production course aims to train students in using appropriate manufacturing techniques and tools, including welding jigs. The use of welding jigs can improve the precision, efficiency, and consistency of welding results, while also reducing the risk of human error. This study aims to design and analyze a welding jig for angular welding in the context of practical coursework at STMI Jakarta Polytechnic. The research methodology includes a literature review, jig design using CAD software, prototype development, and performance testing and analysis of the welding jig. The expected outcomes of the study are to enhance the quality and efficiency of the angular welding process. Additionally, the designed welding jig provides ease of use for students, thereby reducing errors caused by human factors.
Penerapan Single-Minute Exchange of Die (SMED) untuk Penurunan Waktu Setup dan Biaya Produksi pada Injection Molding Sumasto, Fredy; Azzahra, Sabrina; Rangkuti, Indra Yusuf; Imdam, Irma Agustiningsih; Lianny, Indah Kurnia Mahasih; Solih, Edwin Sahrial
Jurnal Optimasi Teknik Industri (JOTI) Vol 7, No 1 (2025)
Publisher : Teknik Industri Universitas Indraprasta PGRI

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.30998/joti.v7i1.27513

Abstract

Waktu setup yang lama pada proses injection molding dapat menyebabkan downtime yang signifikan, mengurangi produktivitas, dan meningkatkan biaya produksi. Penelitian ini bertujuan untuk mengurangi waktu setup mold pada mesin berkapasitas 450 ton di PT MWT dengan menerapkan metode Single Minute Exchange of Dies (SMED). Metode ini diterapkan dengan mengidentifikasi dan mengonversi aktivitas internal menjadi eksternal serta menyederhanakan langkah-langkah aktivitas internal. Hasil penelitian menunjukkan bahwa waktu setup berhasil dikurangi dari 196 menit menjadi 156 menit, menghasilkan pengurangan waktu sebesar 20,4%. Selain itu, biaya produksi harian berkurang sebesar Rp333.333 atau sekitar 20,4% dari total biaya sebelum perbaikan. Peningkatan efisiensi waktu memungkinkan perusahaan untuk meningkatkan kapasitas produksinya tanpa menambah sumber daya. Penerapan metode SMED juga berdampak positif pada kualitas produk, dengan risiko produk cacat yang lebih rendah karena proses setup yang lebih cepat dan terstandardisasi. Penelitian ini menunjukkan bahwa metode SMED merupakan langkah efektif dalam meningkatkan efisiensi dan daya saing perusahaan di industri manufaktur.
Sosialisasi 5R Dan Teknologi Dalam Upaya Meningkatkan Kualitas Dan Keselamatan Pada Bengkel Sepeda Motor Sumasto, Fredy; Imansuri, Febriza; Solih, Edwin Sahrial; Hakim , Ali Rachman; Samudra, Bayu
Journal of Community Services in Sustainability Vol. 2 No. 2 (2024): Journal of Community Services in Sustainability (Oktober 2024)
Publisher : Politeknik STMI Jakarta

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.52330/jocss.v2i2.369

Abstract

Abstract The automotive industry is crucial in urban economies, particularly in densely populated Jakarta. Motorcycle workshops are essential service centers to ensure optimal vehicle functionality and safety. However, many small-scale workshops face challenges maintaining cleanliness, order, and operational efficiency, often affecting service quality. This Community Service Program (PkM) aimed to introduce and implement the 5R principles (Ringkas, Rapi, Resik, Rawat, and Rajin) and appropriate technology in Bahari Motor Service Workshop, Jakarta Timur. The program involved several stages, including initial observations, training on 5R implementation, technology demonstrations, and monitoring and evaluation of outcomes. The results indicated significant improvements in operational efficiency and service quality, with participants demonstrating increased awareness and understanding of the 5R principles. To sustain these improvements, ongoing training and monitoring are recommended. This program benefits the workshop and serves as a model for similar initiatives in the automotive sector, contributing to enhanced service quality and business sustainability. Abstrak Industri otomotif sangat penting dalam perekonomian perkotaan, terutama di Jakarta yang padat penduduknya. Bengkel sepeda motor merupakan pusat layanan yang penting untuk memastikan fungsionalitas dan keamanan kendaraan yang optimal. Namun, banyak bengkel berskala kecil yang menghadapi tantangan dalam menjaga kebersihan, ketertiban, dan efisiensi operasional, yang sering kali mempengaruhi kualitas layanan. Program Pengabdian Kepada Masyarakat (PkM) ini bertujuan untuk memperkenalkan dan menerapkan prinsip 5R (Ringkas, Rapi, Resik, Rawat, dan Rajin) dan teknologi tepat guna di Bengkel Bahari Motor, Jakarta Timur. Program ini melibatkan beberapa tahap, termasuk observasi awal, pelatihan penerapan 5R, demonstrasi teknologi, dan pemantauan dan evaluasi hasil. Hasilnya menunjukkan peningkatan yang signifikan dalam efisiensi operasional dan kualitas layanan, dengan para peserta yang menunjukkan peningkatan kesadaran dan pemahaman tentang prinsip-prinsip 5R. Untuk mempertahankan peningkatan ini, pelatihan dan pemantauan yang berkelanjutan direkomendasikan. Program ini memberikan manfaat bagi bengkel dan menjadi model bagi inisiatif serupa di sektor otomotif, yang berkontribusi pada peningkatan kualitas layanan dan keberlanjutan bisnis.
CLAMPING DIES DESIGN TO MINIMIZE AUTOMOTIVE COMPONENT DIES SETUP TIME AT PT GANDING TOOLSINDO Purbaningrum, Sanurya Putri; Lianny, Indah Kurnia Mahasih; Solih, Edwin Sahrial; Arohman, Abdul Wahid; Satiman , Bayu
Media Mesin: Majalah Teknik Mesin Vol. 25 No. 2 (2024)
Publisher : Universitas Muhammadiyah Surakarta

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.23917/mesin.v25i2.3012

Abstract

PT Ganding Toolsindo was faced with the problem of high automotive component die setup times. The main cause of the high setup time is the process of tightening and releasing the bolts which is done manually. The aim of this research is to design a tool for clamping dies which functions to help speed up the bolt installation process, so that the setup time for automotive component dies is reduced. The method used in this research is field observation followed by the die clamping design process. Design planning begins by drawing the object using CAD software based on the results of load calculations and determining the dimensions of the dies themselves and the press machine as well as selecting the dies material. Furthermore, proof was carried out that this die clamping design could reduce dies setup time using movement analysis with a pre-determined time study Measurement Time Method (MTM) method, where the results showed a time saving of 92.4%.
Penerapan Single Minute Exchange of Dies (SMED) untuk Optimalisasi Proses Pergantian Dies pada Mesin Press SEYI SN2-300 di PT Ganding Toolsindo Purbaningrum, Sanurya Putri; Solih, Edwin Sahrial; Lianny, Indah Kurnia Mahasih; Satiman, Bayu
Journal of Community Services in Sustainability Vol. 3 No. 1 (2025): Journal of Community Services in Sustainability (April 2025)
Publisher : Politeknik STMI Jakarta

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.52330/jocss.v3i1.373

Abstract

Penerapan metode Single Minute Exchange of Dies (SMED) pada mesin press SEYI SN2-300 di PT Ganding Toolsindo bertujuan meningkatkan efisiensi pergantian dies dalam produksi. Tahapan program mencakup analisis proses, sosialisasi, pelatihan, pendampingan, serta evaluasi penerapan SMED. Implementasi menghadapi kendala pada identifikasi aktivitas internal dan eksternal serta adaptasi teknisi terhadap metode baru. Dengan analisis dan pelatihan intensif, beberapa aktivitas internal setup berhasil diubah menjadi eksternal, sehingga waktu setup turun menjadi 29,58 menit dari sebelumnya 35,73 menit. Selain mengurangi downtime, SMED mendukung sistem operasional yang lebih terstruktur, meningkatkan standar kerja, dan kualitas produksi. Evaluasi menunjukkan efektivitas SMED dapat terus ditingkatkan dengan alat bantu tambahan. Implementasi ini tidak hanya meningkatkan efisiensi, tetapi juga membangun budaya kerja disiplin dan berkelanjutan yang mendukung efisiensi waktu, pengurangan biaya, dan peningkatan kualitas produksi.
Comparative Assessment of Spot Welding and Lock Seam on Automotive Inner Tubes for QCDSM and Product Lifecycle Sustainability Nurhadi, Hikari Qurrata'ain; Mustofa, Mustofa; Solih, Edwin Sahrial; Gurning, Ridho Hans
Journal of Mechanical Engineering, Science, and Innovation Vol 5, No 1 (2025): (April)
Publisher : Mechanical Engineering Department - Institut Teknologi Adhi Tama Surabaya

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.31284/j.jmesi.2025.v5i1.7481

Abstract

In the automotive manufacturing industry, enhancing quality and productivity is crucial to meet customer expectations while ensuring safety, environmental sustainability, and energy efficiency. This study evaluates the collapse strength of automotive inner tubes following ISO 2941 standards, comparing lock seam design with SGCC material and resistance spot welding (RSW) applied to SECD material. The findings show that the lock seam process improves structural strength by approximately 20%, due to more uniform pressure distribution, leading to better stability. A key advantage of the lock seam is its spiral construction, which contrasts with RSW's localized spot welds, contributing to more consistent performance. Additionally, the lock seam process reduces production costs and minimizes environmental impact by using thinner, cost-effective SGCC material. It also enables faster production, enhancing delivery efficiency. The absence of welding fumes improves safety conditions and boosts operator morale, while contributing to a cleaner working environment. From a Product Lifecycle Management perspective, this study shows that the lock seam process optimizes design quality, production efficiency, and sustainability, aligning with the goals of Quality, Cost, Delivery, Safety, and Morale (QCDSM). These results support the adoption of lock seam technology for sustainable, efficient automotive manufacturing.
Reduction Cost in Endplate-B Material Component for Oil Filter Bypass System with Redesigning Satria, Adam; Sahrial Solih, Edwin; Putri Purbaningrum, Sanurya; Wahid Arohman, Abdul; Ridho Hans Gurning
Jurnal Serambi Engineering Vol. 10 No. 3 (2025): Juli 2025
Publisher : Faculty of Engineering, Universitas Serambi Mekkah

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Abstract

The bypass system in spin-on type oil filters plays a crucial role in maintaining engine cleanliness and performance by allowing oil to flow when excessive pressure occurs. A critical component of this system is endplate-B, which fulfills dual roles: providing structural support and functioning as an interface for oil passage during bypass operations. However, the relatively high material usage and cost associated with the current design of endplate-B pose challenges in manufacturing efficiency. The objective of this study is to minimize the material cost of endplate-B by optimizing its dimensional geometry without compromising its structural and functional performance. The research methodology encompasses dimensional redesign, structural analysis, and performance validation under simulated operating conditions. The findings indicate that strategic dimensional modifications can substantially reduce material usage while preserving mechanical strength and functional integrity. The implementation of this optimized design provides a cost-effective solution for the manufacturing of oil filters and contributes to broader efforts to improve production efficiency in the automotive component industry.
Perancangan dan Analisis Welding fixture untuk Pengelasan Part Cushion Seat Frame di PT Laksana Tekhnik Makmur Putri, Sanurya; Johannnes; Sahrial Solih, Edwin; Fadlurrohman Nurhadi, Fadhil
J-Proteksion: Jurnal Kajian Ilmiah dan Teknologi Teknik Mesin Vol. 9 No. 2 (2025): J-Proteksion
Publisher : Universitas Muhammadiyah Jember

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.32528/jp.v9i2.2707

Abstract

PT Laksana Tekhnik Makmur menghadapi kendala dalam menjaga konsistensi kualitas dan efisiensi proses pengelasan cushion seat frame akibat variasi hasil dari pengelasan manual. Untuk meningkatkan efisiensi dan kualitas, penelitian ini mengembangkan welding fixture yang tepat. Metodologi meliputi studi literatur, identifikasi produk, perancangan fixture, simulasi, dan analisis menggunakan perangkat lunak Finite Element Analysis (FEA). Hasil desain welding fixture berukuran 900 mm x 400 mm x 150 mm, tanpa clamp, dan menggunakan material SPHC serta SS 400 yang memenuhi standar kualitas dan titik kritis produk. Simulasi menunjukkan tegangan maksimum 0,816 MPa dengan sebaran minimum dan displacement tertinggi 0,007 mm dalam sebaran minimum. Faktor keamanan terendah adalah 15, lebih tinggi dari batas minimum yang diizinkan (nilai batas minimum 1). Yield strength material SPHC dan SS 400 masing-masing sebesar 248,225 MPa dan 344,756 MPa, serta tegangan von mises maksimum 0,816 MPa. Kesimpulan dari hasil analisis bahwa desain welding fixture aman dan efektif untuk digunakan dalam meningkatkan efisiensi dan konsistensi kualitas proses pengelasan di PT Laksana Tekhnik Makmur.
Reduction Cost in Material Spring-type Coil for Heavy-duty Oil Filter By-pass System with Redesigning Solih, Edwin Sahrial; Gurning, Ridho Hans; Satria, Adam; Edwin Sahrial Solih; Purbaningrum, Sanurya Putri; Arohman, Abdul Wahid; Ridho
Infotekmesin Vol 16 No 2 (2025): Infotekmesin: Juli 2025
Publisher : P3M Politeknik Negeri Cilacap

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.35970/infotekmesin.v16i2.2665

Abstract

The bypass system in oil filters plays a crucial role in maintaining engine cleanliness and performance by allowing oil to flow through the filter when the pressure exceeds set limits. A critical component of this system is the coil spring that controls the bypass valve. In this study, an experimental approach was applied to reduce material cost while preserving performance. We redesigned the spring from four coils of 3.5 mm diameter to three coils of 3 mm diameter, using the same standard hard steel wire SW‑C. The redesigned springs were subjected to a standard impulse test of 250,000 cycles under 7 kgf/cm² pressure and a loading test with deflections from 1 to 10 mm at pressures up to 11 kgf. Results show that the new three‑coil SW‑C spring meets all performance criteria: impulse life and load‑deflection characteristics fall within standard tolerances. A direct comparison with the original design demonstrates negligible differences in functional behavior, confirming that material usage and costs can be reduced without sacrificing reliability. These findings offer valuable guidance for the cost‑efficient production of oil filter components in automotive engineering.
Reduction Cost in Material Spring-type Coil for Heavy-duty Oil Filter By-pass System with Redesigning Solih, Edwin Sahrial; Gurning, Ridho Hans; Satria, Adam; Edwin Sahrial Solih; Purbaningrum, Sanurya Putri; Arohman, Abdul Wahid; Ridho
Infotekmesin Vol 16 No 2 (2025): Infotekmesin: Juli 2025
Publisher : P3M Politeknik Negeri Cilacap

Show Abstract | Download Original | Original Source | Check in Google Scholar | DOI: 10.35970/infotekmesin.v16i2.2665

Abstract

The bypass system in oil filters plays a crucial role in maintaining engine cleanliness and performance by allowing oil to flow through the filter when the pressure exceeds set limits. A critical component of this system is the coil spring that controls the bypass valve. In this study, an experimental approach was applied to reduce material cost while preserving performance. We redesigned the spring from four coils of 3.5 mm diameter to three coils of 3 mm diameter, using the same standard hard steel wire SW‑C. The redesigned springs were subjected to a standard impulse test of 250,000 cycles under 7 kgf/cm² pressure and a loading test with deflections from 1 to 10 mm at pressures up to 11 kgf. Results show that the new three‑coil SW‑C spring meets all performance criteria: impulse life and load‑deflection characteristics fall within standard tolerances. A direct comparison with the original design demonstrates negligible differences in functional behavior, confirming that material usage and costs can be reduced without sacrificing reliability. These findings offer valuable guidance for the cost‑efficient production of oil filter components in automotive engineering.